The inards did not look too bad, pull all the parts, plunger, spring, rubber gaskets, etc. I pulled the top resivour off, and unscrewd the brake switch.
There was some rust on the inside, so I soaked in 100% vinegar for two hours. This cleaned it up nice, and I soaked with thin oil to keep it from rusting again.
Cleaned up all the parts and re-assembled, re-installed, and bam no brake pressure. I will buy a rebuild kit as air seems to be seeping through at this point.
Here is the rebuild kit, $69.00
Picture of ORIGINAL internal plunger for reference